爆破2024,Vol.41Issue(1) :106-111,133.DOI:10.3963/j.issn.1001-487X.2024.01.015

复合结构嵌套建(构)筑物一次性爆破拆除

One-time Blasting Demolition of Nested Building(Structure)with Composite Structure

周晓光 孙向阳 周明安 谢续文 陈茂维
爆破2024,Vol.41Issue(1) :106-111,133.DOI:10.3963/j.issn.1001-487X.2024.01.015

复合结构嵌套建(构)筑物一次性爆破拆除

One-time Blasting Demolition of Nested Building(Structure)with Composite Structure

周晓光 1孙向阳 2周明安 1谢续文 2陈茂维2
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作者信息

  • 1. 湖南铁军工程建设有限公司,长沙 410003
  • 2. 湖南中人爆破工程有限公司,长沙 410003
  • 折叠

摘要

针对43 m高钢结构锅炉框架崁套建筑物的爆破拆除,对2~6号锅炉房5个锅炉框架采取一次性定向爆破的方法拆除,按2~6号锅炉房顺序由北到南逐跨向东倒塌.对钢筋混凝土支撑柱实施钻孔爆破;锅炉框架采用聚能切割器,对钢结构的支撑柱进行切割爆破.2号、3号锅炉第一排支撑柱切口高6 m,设置3个切口;第二排支撑柱切口高为4.0 m,设置3个切口;第三排支撑柱的切口高为3.0 m,设置2个切口.4~6号锅炉支撑框架第一排支撑柱切口 6 m,第二排支撑柱切口 3.5 m.使用SGPQ-15型(180 g/m)切割器切割14 mm厚度以下钢板,SGPQ-19型(280 g/m)切割器切割16 mm和20 mm厚度钢板,总装药量30.288 kg.爆破时,煤斗间、锅炉厂房屋顶、钢结构锅炉框架按设计方向倾覆.起爆瞬间2号锅炉框架下沉,0.25 s后锅炉房5号柱下座,随后按0.25 s的起爆间隔,厂房由北向南逐跨坍塌向东定向倾倒.两个楼梯间在剪力墙的支撑下明显坍塌滞后,在锅炉翻转的冲击下向东倾倒.锅炉房东侧立柱向东侧倾倒过程中,上下爆破切口间立柱被压缩坍塌,立柱距离烟囱16 m,中间楼梯、锅炉及剪力墙上部向前倾倒,主体距离烟囱14 m,塌散物距离烟囱最近6 m.爆破飞石和爆破振动(0.28 cm/s)均未超标,未对周边的建筑物和设施造成任何损坏.

Abstract

Aiming at the blasting demolition of the buildings embedded with a 43 m high steel structure boiler frame,the five boiler frames of No.2~No.6 boiler rooms were demolished by one-time directional blasting method and collapsed from north to south by span to east according to the order of No.2~No.6 boiler rooms.The reinforced concrete support columns were drilled and blasted,and the steel support columns were cut by a shaped energy cutter.Three cuts for the first-row of support columns of No.2 and No.3 boilers were set with a cut heigh of 6 m.Similarly,three 4m high cuts and two 3 m high cuts were set for the second-row and the third-row of support columns,respec-tively.The cut heights of the first-row and second-row of support columns of No.4~No.6 boilers were set as 6 m and 3.5 m,respectively.Additionally,the steel plates with a thickness less than 14 mm were cut by the SGPQ-15(180 g/m)cutter,and the steel plates with a thickness of 16mm and 20 mm were cut by the SGPQ-19(280 g/m)cutter.The total charge was 30.288 kg.During the explosion,the coal hopper room,boiler building roof and steel structure boiler frame overturned according to the designed direction.The frame of No.2 boiler sank at the moment of detonation,and the lower seat of No.5 column in the boiler room was placed after 0.25 seconds.Subsequently,the factory collapsed span by span from north to south and tilted towards the east with a detonation interval of 0.25 sec-onds.The collapse of the two stairwells were lagged significantly under the support of shear walls,and the stairwells toppled eastward under the impact of boiler overturning.The column between the upper and lower blasting cuts was compressed and collapsed during the tilting process of the column on the east side of the boiler room towards the east.The column was 16 m away from the chimney,and the upper part of the middle staircase,boiler,and shear wall were tilted forward.The main body was 14 m away from the chimney,and the closest distance of collapsed object to the chimney was 6 m.Both of the blasting flying stones and blasting vibration(0.28 cm/s)did not exceed the stand-ard,and the blasting demolition did not cause any damage to surrounding buildings and facilities.

关键词

复合结构/嵌套建筑/爆破拆除

Key words

composite structure/nested buildings/blasting demolition

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出版年

2024
爆破
湖北省爆破学会 武汉理工大学

爆破

CSTPCDCSCD北大核心
影响因子:1.052
ISSN:1001-487X
参考文献量32
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