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某1000 MW超超临界二次再热机组ATT跳闸原因分析及措施

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某1 000MW超超临界二次再热机组在进行阀门活动性试验(ATT)时,控制(EH)油压异常下降,随后汽轮机所有调节阀全关,触发了发电机逆功率保护,导致机组跳闸.基于油动机工作原理和数字式电液调节系统(DEH)逻辑中存在的调节阀防卡涩逻辑对该机组跳闸事件原因进行分析,并且提出处理建议及后续的防范措施.结果表明:通过严格控制EH油油质、优化试验流程、加强逻辑组态检查,可以有效避免ATT导致汽轮机跳闸.研究结果对同类型发电机组的调试及运行具有一定的参考意义.
Cause Analysis and Measures of Tripping During ATT of a 1000 MW Ultra-supercritical Double Reheat Unit
A 1 000 MW ultra-supercritical double reheat unit experienced an abnormal drop in control(EH)oil pressure during a valve activity test(ATT),which led to the closure of all turbine control valves,triggering the generator reverse power protection and causing the unit to trip.The causes of the accident were analysed,and the treatment suggestions and subsequent preventive measures were put forward based on the working principle of the oil motor and the control valve anti-jamming logic in the logic of the digital electrohydraulic control system(DEH).Results show that,by strictly controlling the quality of EH oil,optimizing the test process,and enhancing the inspection of logic configurations,the turbine trip caused by ATT can be effectively avoided.The research results have a certain reference significance for the commissioning and operation of similar types of units.

ultra-supercritical unitdouble reheatATTEH oil pressurecontrol valveanti-jamming logic

陈鑫

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江苏国信沙洲发电有限公司,江苏张家港 215600

超超临界机组 二次再热 ATT EH油压 调节阀 防卡涩逻辑

2025

发电设备
上海发电设备成套设计研究院

发电设备

影响因子:0.26
ISSN:1671-086X
年,卷(期):2025.39(1)