广东化工2024,Vol.51Issue(19) :57-59.DOI:10.3969/j.issn.1007-1865.2024.019.018

致密气藏气井解堵剂性能评价及应用效果分析

Performance Evaluation and Application Effect Analysis of Plug Removal Agents for Tight Gas Reservoirs and Gas Wells

邹春霞 杨丽 邹天赐 夏海英 赵祥 王坤
广东化工2024,Vol.51Issue(19) :57-59.DOI:10.3969/j.issn.1007-1865.2024.019.018

致密气藏气井解堵剂性能评价及应用效果分析

Performance Evaluation and Application Effect Analysis of Plug Removal Agents for Tight Gas Reservoirs and Gas Wells

邹春霞 1杨丽 1邹天赐 1夏海英 1赵祥 1王坤1
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作者信息

  • 1. 中国石化股份有限公司西南油气分公司石油工程技术研究院,四川 德阳 618000
  • 折叠

摘要

针对致密气藏部分气井井筒堵塞,导致产量下降的问题,开展了水质分析和堵塞物成分分析,并开发和评价一种适应该区块的解堵剂.产品室内评价结果表明:配伍性良好;能有效溶解储层堵塞物;不同温度下该产品16 h对堵塞物溶解率可达到80%以上,对管柱腐蚀低,符合行业一级要求指标;具有较强的螯合成垢离子能力.解堵剂现场应用良好,解除了井筒堵塞,平均单井日产气量提高了0.73 万方/天.

Abstract

In view of the problem that some gas Wells in tight gas reservoirs,which leads to the decline of production,the water quality analysis and the composition analysis of the blockage are carried out,and a kind of plugging agent suitable for this block is developed and evaluated.The results of indoor evaluation show that:good compatibility;Can effectively dissolve reservoir plugging;Under different temperatures,the dissolution rate of the plugging material in 16 h can reach more than 80%,and the corrosion of the pipe string is low,which meets the industry level 1 requirements.It has strong chelating ability to synthesize scale ions.The plugging agent was well applied to the field and the blockage was removed,increasing the average daily gas production per well by 7,300 m3/d.

关键词

苏里格/井筒堵塞/解堵剂/性能评价/现场应用

Key words

sulige/wellbore blockage/plugging remover/performance evaluation/field application

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基金项目

中石化西南油气分公司石油工程技术研究院项目(GCY2019-501-YHYJ)

出版年

2024
广东化工
广东省石油化工研究院

广东化工

影响因子:0.288
ISSN:1007-1865
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