首页|水电机组水导油槽油混水超标原因分析

水电机组水导油槽油混水超标原因分析

扫码查看
高坝洲水电站 3 号机组在C修后,运行过程中出现水导油槽油混水超标问题,检查发现水导油槽盖板接触式梳齿密封与大轴之间配合不佳、存在较大间隙.进一步观察分析表明,因为间隙使油槽内外空气出现热交换,导致在密封和大轴配合处出现聚集的冷凝水,冷凝水顺着大轴流入油槽内,经过长时间的积累,最终导致油槽油混水超标,通过更换密封、清扫油槽、更换新油等措施,解决了问题.
Analysis of Excessive Water Mixing in Water Guide Bearing Oil Groove of Hydro-turbine Units
Excessive water mixing in the oil in water guide bearing oil groove is observed in the No.3 unit in Gaobazhou Hydropower Station after the C-level maintenance.Inspection shows that the contact type comb tooth seal of the cover plate of the water guide bearing oil groove does not fit well with the main shaft that a large clearance is found.Further observation and analysis show that heat exchange occurs between the air inside and outside the oil groove due to the clearance,resulting in the accumulation of condensed water at the contact place of the seal and the main shaft.The con-densed water then flows into the oil groove along the shaft.After the accumulation of a long period,it ultimately leads to excessive water mixing in the oil.By replacing the seal,cleaning the oil tank,and replacing the oil,the problem is fi-nally solved.

water guide bearing oil tankoil mixed with watercomb tooth sealheat exchange

周敏、张言、周金路、刘永钊、毛彦杰

展开 >

湖北清江水电开发有限责任公司,湖北 宜昌 443000

水导油槽 油混水 梳齿密封 热交换

2024

水电与新能源
湖北省水力发电工程学会 湖北能源集团股份有限公司

水电与新能源

影响因子:0.301
ISSN:1671-3354
年,卷(期):2024.38(8)