Regarding the issue of high water injection pressure and inability to meet the designated injection volume in a certain block of the X oilfield,the reasons for under-injection were analyzed based on factors such as reservoir characteristics,formation oil-water properties,and water quality of injections.Based on this analysis,a management approach was adopted that encompassed measures such as relieving blockages,preventing clay expansion,stabilizing and consolidating sand,and reducing pressure to enhance capacity.To achieve this,techniques for sand consolidation and blockage removal were applied in loose sandstone,thus presenting a new avenue for balancing the injection-production relationship.
关键词
注水井/稳砂解堵/降压增注
Key words
water injection well/stable sand/clay and unblocking/reduce blood pressure and increase injection