首页|提升导热油系统电气化率的优化技术

提升导热油系统电气化率的优化技术

扫码查看
以某炼化企业的甲乙酮装置2 326 kW高温热媒炉电气化改造作示范,设计1套电加热导热油系统,包括电加热导热油炉、供电系统及工艺改造等,替代原有热媒炉系统.电加热系统通过使用绿电技术,预计热效率超过95%,同时可减少CO2排放4 716 t/a,终端电气化率提升了10.99%,具有非常显著的绿色减排效果.该示范项目的开展,为甲乙酮装置其它加热炉改造提供技术依托,也为炼化企业大范围的电气化率改造提供参考.同时,装置电气化率的提升,对统筹优化全厂的电力、热力供应,保障炼化装置的安全稳定运行起到了推进作用.
Optimization technology for improving electrification rate of thermal oil system
Taking the electrification transformation of a 2326 kW high temperature heat medium furnace of a methyl ethyl ketone unit in a refining and chemical company as a demonstration,a set of electric heating thermal oil system was designed,including electric heating thermal oil furnace,power supply system and process transformation,to replace the original heat medium furnace system.Through the use of green-power technology,the electric heating system was expected to have a thermal efficiency of more than 95%,while reducing CO2 emissions of 4 716 t/a,improving the terminal electrification rate to 10.99%,which had a very significant green emission reduction effect.The development of this demonstration project provided technical support for the transformation of other heating furnaces of methyl ethyl ketone unit,and also provided reference for the transformation of electrification rate in a wide range of refining and chemical companies.At the same time,the improvement of the electrification rate of the plant had played a role in promoting the overall optimization of the power and heat supply of the whole plant and ensuring the safe and stable operation of the refining and chemical plant.

electric heating furnacehigh temperature heat medium furnacetransformationcarbon emissionselectrification rate

陈世龙、杨俊明、张霖、马军、王瑞、张寰

展开 >

中国石油兰州石化公司,甘肃 兰州 730060

电加热炉 高温热媒炉 改造 碳排放 电气化率

2024

炼油与化工
黑龙江省石油学会,大庆石化公司

炼油与化工

影响因子:0.185
ISSN:1671-4962
年,卷(期):2024.35(6)