The original water inrush coefficient of the floor aquifer of the 9303 working face of Xipang well is 0.094~0.126 MPa/m.The high confined aquifer seriously threatens the safe production of the working face.The method of theoretical analysis is used to determine the design depth of reconstruc-tion section of floor confined water for ground regional treatment is 12.0~25.0 m.The thickness of the renovated waterproof layer is 51.0~64.0 m.The water inrush coefficient after renovation is 0.081~0.076 MPa/m.The treatment effect of floor confined water is evaluated through field measure-ment.The results show that the actual reconstruction depth of the floor confined water is 10.7~24.2 m.The actual thickness of the renovated waterproof layer is 50.8~64.3 m.The final pressure of the grouting section is above 6 MPa,and the pump volume reaches below 35 L/min at the end of grou-ting,which meets the grouting standard.The water inrush coefficient after treatment of floor aquifer is 0.073~0.085 MPa/m,less than 0.100 MPa/m,which meets the requirements of safe mining in working face.
coal miningfloor confined waterground regional treatmentthickness of the renovated wa-terproofwater inrush coefficient