江西建材2024,Issue(3) :71-72,79.

高延性混凝土局部置换加固剪力墙抗震性能试验分析

Analysis of Seismic Performance of Shear Wall with High Ductility Concrete

赵艳梅
江西建材2024,Issue(3) :71-72,79.

高延性混凝土局部置换加固剪力墙抗震性能试验分析

Analysis of Seismic Performance of Shear Wall with High Ductility Concrete

赵艳梅1
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作者信息

  • 1. 吕梁市建筑勘察设计院,山西 吕梁 033000
  • 折叠

摘要

为探究高延性混凝土在提升剪力墙抗震性能方面的作用,文中研究制备了改性活性粉末混凝土,其中添加了聚丙烯纤维和钢纤维.制作三组剪力墙试件,利用高延性混凝土对第三组试件进行局部置换加固,另外两组作为对照组.通过向试件施加垂直载荷与水平载荷模拟地震作用,观察其破坏形态、位移量、钢筋应变.经对比可知,加固试件的承载能力、变形消能效果均强于对照组,说明加固后的剪力墙具有更好的抗震性能.

Abstract

In order to explore the role of high-ductile concrete in improving the seismic performance of shear wall,the modified active powder concrete is prepared,in which polypropylene fiber and steel fiber are added.Three sets of shear wall specimens were made,and the third set of specimens were partially replaced and reinforced by high-tensile concrete,and the other two sets were used as control groups.Apply vertical load and horizontal load to the specimen,and observe the damage form,displacement and reinforcement strain.After comparison,the bearing capacity and deformation and energy dissipation effect of the reinforced specimen are stronger than that of the control group,indicating that the reinforced shear wall has better seismic performance.

关键词

高延性混凝土/局部置换加固/剪力墙/抗震性能

Key words

High-ductile concrete/Partial replacement and reinforcement/Shear wall/Seismic performance

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出版年

2024
江西建材
江西省建材科研设计院

江西建材

影响因子:2.247
ISSN:1006-2890
参考文献量6
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