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柴油加氢改质装置节能措施效果评估

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河南丰利石化有限公司建有60 万t·a-1 中芳烃加氢改质装置,设计操作压力为13.4 MPa,设计能耗为每吨原料油20.29 kg标油,高于中石化同类装置的能耗定额(每吨原料油12 kg标油),其中电耗占该装置总能耗的 60%.该装置通过投用热进料、新氢压缩机增加无级调节系统、循环氢压缩机增加无级调节系统、高压胺液泵加装变频器等节能措施,达到该装置节能降耗的目的,产生了良好的经济效益.
Effect Evaluation of Energy Saving Measures for Diesel Hydrotreating Unit
Henan Fengli Petrochemical Co.,Ltd.has built a 0.6 Mt·a-1 mid-aromatics hydro-upgrading unit with a designed operating pressure of 13.4 MPa and a designed energy consumption of 20.29 kg standard oil per 1 t feedstock oil,which is higher than the energy consumption quota of similar units in Sinopec(12 kg standard oil per 1 t raw oil),in which electricity consumption accounts for 60%of the total energy consumption of the device.The device achieves the purpose of saving energy and reducing consumption by using hot feed,adding a stepless regulation system to a new hydrogen compressor,adding a stepless regulation system to a circulating hydrogen compressor,and adding a frequency converter to the high-pressure amine pump.Good economic benefits have been obtained.

Diesel hydrogenationEnergy savingStepless air volume adjustmentInverterHot feeding

马社忠、马可望

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濮阳石油化工职业技术学院,河南 濮阳 457000

柴油加氢 节能 无级气量调节 变频器 热进料

2024

辽宁化工
辽宁省化工学会

辽宁化工

影响因子:0.234
ISSN:1004-0935
年,卷(期):2024.53(1)
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