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W火焰锅炉SCR脱硝超低排放技术及应用

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截至2021年底,全国已有超过 95%的燃煤火电机组实现了氮氧化物超低排放,剩余均为燃用无烟煤的W火焰锅炉,其产生的氮氧化物质量浓度高达 750~1 200 mg/m3,实现超低排放难度大,是我国实现超低排放政策的"最后一公里".目前,选择性催化还原(SCR)脱硝流场技术主要有"SCR分区混合动态调平技术""全烟道断面混合流场技术""常规精准喷氨技术"等.以某设计脱硝效率需高达 95%的 W 火焰锅炉为例,通过计算流体力学(CFD)模拟的方式对比 3 种技术的性能指标,"SCR分区混合动态调平技术"的各项指标明显优于其他技术.工程改造后,在脱硝系统入口氮氧化物质量浓度为1 000 mg/m3,出口低于50 mg/m3 时,可实时保持氨逃逸量小于 3 μL/L,远超常规SCR脱硝系统最高设计效率(93%),为W火焰锅炉氮氧化物超低排放提供了新的技术路线.
Ultra low emission technology of SCR flue gas denitration in W-flame boiler and the application
By the end of 2021,over 95%of coal-fired thermal power units in China have achieved ultra-low emission of nitrogen oxides,with the remaining being W-flame boilers that burn anthracite.Due to the high mass concentration of nitrogen oxides generated,which often reaches 750~1 200 mg/m3,achieving ultra-low emissions is difficult,making it the"last mile"for China to achieve ultra-low emission policies.At present,selective catalyst reduction(SCR)denitration flow field technology mainly includes"SCR partition hybrid dynamic leveling technology","full flue section mixing flow field technology",and"conventional accurate ammonia injection technology",etc.Taking a W-flame boiler of which the design denitration efficiency needs to be up to 95%as an example,this paper compares the performance indicators of various technologies through CFD simulation,and the indicators of the"SCR partition hybrid dynamic leveling technology"are significantly superior to other technologies.After the project transformation,when the mass concentration of nitrogen oxides at the denitration system inlet is 1 000 mg/m3 and that at the system outlet is lower than 50 mg/m3,the ammonia escape can be kept less than 3 μL/L,far exceeding the maximum design efficiency of the conventional SCR denitration system.The research provides a new technical route for ultra-low NOx emission of W-flame boilers.

W-flame boilerdenitrationSCRflow field optimizationammonia escapezone mixing

罗志、王晓冰、潘栋、何育东、晋中华、尚桐、范玮、邓彪、任建永、兰永胜、杨小金、杨晓刚、李淑宏

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西安热工研究院有限公司,陕西 西安 710054

西北工业大学动力能源学院,陕西 西安 710129

华能海南发电股份有限公司,海南 海口 572631

华能山东发电有限公司,山东 济南 250013

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W火焰锅炉 脱硝 SCR 流场技术 氨逃逸 分区混合

中国华能集团有限公司总部科技项目中国华能集团有限公司总部科技项目陕西省重点研发计划

HNKJ21-H46HNKJ22-HF482023-YBGY-289

2024

热力发电
西安热工研究院有限公司,中国电机工程学会

热力发电

CSTPCD北大核心
影响因子:0.765
ISSN:1002-3364
年,卷(期):2024.53(3)
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