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安钢永通公司烧结烟气脱硫脱硝工艺优化实践

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烧结烟气在基准φ(O2)为16%的条件下,颗粒物、二氧化硫、氮氧化物排放质量浓度需分别不高于10 mg/m3、35 mg/m3、50 mg/m3.安钢集团永通球墨铸铁管有限责任公司为响应新要求,对其105 m2烧结机进行了技术升级,淘汰原有湿法脱硫工艺,新建一套活性炭烟气脱硫脱硝净化装置.活性炭脱硫脱硝净化装置投用前期运行良好,但随着运行时间的增长,逐渐出现净化塔温度超温、净化塔床层阻力过高、制酸效率低等问题,制约烧结生产.后通过工艺升级和设备优化改造,实现了活性炭脱硫脱硝装置的稳定运行,并显著提高了脱硫脱硝效率,降低了烧结烟气中的污染物排放,为类似企业的烟气治理提供了参考和借鉴.
Optimization Practice of Sintering Flue Gas Desulfurization and Denitrification Process in Angang Yongtong Company
Under the condition of a benchmark φ(O2)of 16%,the emission mass concentrations of particulate matter,sulfur dioxide,and nitrogen oxides in sintering flue gas should not exceed 10 mg/m3,35 mg/m3,and 50 mg/m3,respectively.In response to new requirementss,Angang Group Yongtong Ductile Iron Pipe Co.,Ltd.has upgraded its 105 m2 sintering machine,eliminated the original wet desulfurization process,and built a new set of activated carbon flue gas desulfurization and denitrification purification device.The activated carbon desulfurization and denitrification purification device operated well in the early stage of operation,but as the operating time increased,problems such as overheating of the purification tower,high bed resistance of the purification tower,and low acid production efficiency gradually emerged,which restricted sintering production.Through process upgrades and equipment optimization,the stable operation of the activated carbon desulfurization and denitrification device was achieved,and the desulfurization and denitrification efficiency was significantly improved,reducing pollutant emissions in sintering flue gas and providing reference and inspiration for similar enterprises'flue gas treatment.

activated carbondesulfurization and denitrificationprocess optimizationoperational practice

申海峰、王迎坤、王景

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安钢集团永通球墨铸铁管有限责任公司,河南 安阳 455100

活性炭 脱硫脱硝 工艺优化 运行实践

2024

山西冶金
山西省金属学会 山西省有色金属学会

山西冶金

影响因子:0.139
ISSN:1672-1152
年,卷(期):2024.47(8)