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渤中油田某井通井钻具卡钻原因浅析及认识

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这篇文章以渤海油田某井卡钻案例为例详细分析了卡钻原因和处理过程.从地层因素、工程因素和人员评估等多个角度阐述了导致卡钻的复杂情况.对类似情况的建议包括加强钻井液循环、详细评估钻井液性能、提前进行井壁稳定性测试等,以预防类似事故再次发生,为类似卡钻事故处理及预防提供一定的借鉴意义.
A Brief Analysis of the Reasons for Stuck Drilling Pipe in a well within the Bohai Oilfield
This paper extensively analyzes a drilling incident in a well within the Bohai oilfield,focusing on an 8-1/2"borehole section.It provides a comprehensive examination of the causes and management of the drilling blockage from both subjective and objective perspectives.The analysis revolves around geological,engineering,and personnel-related factors contributing to the complex situation.Recommendations proposed encompass measures such as optimizing mud circulation,conducting thorough assessments of drilling fluid properties,and pre-emptive stability testing of borehole walls.These suggestions aim to mitigate and prevent similar incidents in future drilling operations.

Bohai oilfieldStuck drilling pipeCause analysisPrevent measures

张彦军

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中海油田服务股份有限公司 天津 300452

渤中油田 卡钻 原因分析 预防措施

2024

石化技术
中国石化集团资产经营管理有限公司北京燕山石化工分公司

石化技术

影响因子:0.261
ISSN:1006-0235
年,卷(期):2024.31(2)
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