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抗盐聚合物污水配聚体系驱油可行性实验研究

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通过不同水质抗盐聚合物污水配聚体系回注1000mD岩心的流动性实验,以渗透率损失率评价配聚体系对岩心的伤害程度,确定了其注入界限并通过驱油实验评价了驱油效果,研究结果对抗盐聚合物污水配聚回注的油层保护和提高采收率具有积极作用.
Experimental study on the feasibility of salt resistant polymer wastewater blending system for oil displacement
This article designed a flowability experiment for the reinjection of 1000mD rock core with different water quality salt resistant polymer wastewater blending systems.The degree of damage caused by the blending system to the core was evaluated based on permeability loss rate,and its injection boundary was determined.The oil displacement effect was evaluated through oil displacement experiments.The research results showed that the oil layer protection and enhanced oil recovery of salt resistant polymer wastewater blending reinjection have a positive effect.

Salt resistant polymer wastewaterPermeability lossOil layer protectionOil displacement effectImproving oil recovery

寇子健、黄立凯

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中海石油(中国)有限公司 北京 100010

中海浙江宁波液化天然气有限公司 浙江 宁波 315000

抗盐聚合物污水 渗透率损失 油层保护 驱油效果 提高采收率

2024

石化技术
中国石化集团资产经营管理有限公司北京燕山石化工分公司

石化技术

影响因子:0.261
ISSN:1006-0235
年,卷(期):2024.31(2)
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