首页|BLX潜山油藏CO2注气试验研究

BLX潜山油藏CO2注气试验研究

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开展潜山油藏CO2注气试验研究,选用35 MPa CC级井口、Y441耐高温高压气密封隔器、BGT3型气密扣油管进行高温深层液态CO2注入;通过室内实验明确CO2腐蚀机理,采用封隔器卡封、环空替入保护液的方式保护上部套管,环空保护液选用了HZ-4缓蚀剂.现场试验验证了注气管柱的可靠性,累计注入液态CO21.3×104 t,对应油井阶段增油800 t以上,表明雾迷山潜山油藏注入性良好,具备大规模埋存CO2的条件,同时证明了CO2驱提高采收率的可行性,潜山油藏开展大规模碳埋存、碳驱油,对于助力我国实现碳达峰、碳中和具有重要意义.
Experimental study on CO2 injection in BLX Buried Hill Reservoir
An experimental study on CO2 injection in buried hill reservoirs was conducted.A 35 MPa,CC level wellhead,Y441 high-temperature and high-pressure gas sealing packer,and BGT3 type airtight buckle oil pipe were selected for high-temperature and deep liquid CO2 injection.The mechanism of CO2 corrosion was clarified through indoor experiments,and the upper casing was protected by employing a packer to seal and replacing the annulus with protective fluid.The formulation of the corrosion inhibitor for the annulus protection fluid is designed as HZ-4.The reliability of the gas injection pipe string was verified through experiments.The cumulative injection of 13 000 tons of liquid CO2 corresponds to the oil increase of more than 800 t in the oil well stage,which shows that the buried hill reservoir of Wumishan has good injectivity and the conditions for large-scale CO2 storage.It also proves the feasibility of CO2 flooding to improve oil recovery,which is of great significance for the buried hill reservoir to carry out large-scale carbon storage and carbon flooding and help China achieve carbon peaking and carbon neutrality.

carbon storagecarbon floodinggas injection pipe stringcorrosion protection of casing

杜航、李栋、朱治国、侯东星、谷胜群

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中国石油华北油田公司第三采油厂,河北沧州 062450

碳埋存 碳驱油 注气管柱 套管防腐

2024

石油工程建设
中国石油集团海洋工程有限公 中国石油工程建设公司

石油工程建设

影响因子:0.367
ISSN:1001-2206
年,卷(期):2024.50(3)