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连续管套管除垢空化射流喷头优化设计与应用

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采用常规方法解决大庆油田油水井结蜡、结垢严重的问题,以及其射孔层段炮眼附近堵塞等引发的单井产液量下降、水井不吸水等问题,具有施工效率低、费用高、作业周期长的缺点.为此,通过优选空化射流喷嘴类型,开展空化射流靶距和角度的优化研究,计算喷嘴使用参数,再通过数值模拟的方式验证该喷头在小直径连续管套管除垢空化射流的效果;同时,制定炮眼除垢选井原则,优化连续管除垢工艺参数.通过结垢结蜡套管除垢、射孔层段炮眼除垢等现场应用表明,连续管套管除垢空化射流喷头在套管内和射孔层段炮眼除垢效果明显.所得结论可为解决油水采出井套管除垢工具研制与工艺参数优选提供借鉴.
Optimized Design and Application of Cavitation Jet Nozzle for CT Casing Descaling
In Daqing Oilfield,conventional techniques are inefficient,costly and time-consuming in dealing with the problems of sever waxing and scaling of oil/water production wells,as well as declining single-well liquid production and failed water adsorption of water production well caused by blockage near the perforations.To solve these problems,the cavitation jet target distance and angle were optimized by using optimal type of cavitation jet nozzle.The nozzle parameters were determined,and then the performance of the nozzle in cavitation jetting for cas-ing descaling of small diameter coiled tubing was verified through numerical simulation.Moreover,the principles of well selection for perforation descaling were defined,and the parameters of descaling process by small diameter coiled tubing were optimized.Field applications have revealed outstanding performance in casing descaling and per-foration descaling.The conclusions provide reference for tool development and process parameter optimization for casing descaling in oil/water production wells.

cavitation jet nozzlecasing descalingperforation descalingwaxingscalingCT technology

刘锴沅

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大庆油田第三采油厂

空化射流喷头 套管除垢 炮眼除垢 结蜡 结垢 连续管技术

中国石油天然气集团有限公司科学研究与技术开发项目

2017B-4107

2024

石油机械
中国石油天然气集团公司装备制造分公司 中国石油学会石油工程专业委员会 江汉机械研究所 江汉石油管理局

石油机械

CSTPCD北大核心
影响因子:0.737
ISSN:1001-4578
年,卷(期):2024.52(2)
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