仪器仪表用户2024,Vol.31Issue(4) :90-92.DOI:10.3969/j.issn.1671-1041.2024.04.031

基于凝汽器乏汽外引改造的余热供热技术应用

Application of Waste Heat Heating Technology Based on Condenser Drain-out Transformation

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仪器仪表用户2024,Vol.31Issue(4) :90-92.DOI:10.3969/j.issn.1671-1041.2024.04.031

基于凝汽器乏汽外引改造的余热供热技术应用

Application of Waste Heat Heating Technology Based on Condenser Drain-out Transformation

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作者信息

  • 1. 内蒙古电力勘测设计院有限责任公司,内蒙古呼和浩特 010020
  • 折叠

摘要

火力发电厂的乏汽余热回收供热可以大大降低机组冷端损失.本文提出了一种乏汽引出后利用增汽机引射乏汽供热的方法对电厂机组进行改造.结论表明,在额定工况下可回收 589 t/h乏汽潜热,降低 2 号机组年平均发电标煤耗61 g/(kW·h),增加全厂供热能力 131 MW,增加供热面积 262 万m2.机组供热能力经过乏汽改造提高了 131 MW,供热量增加了134万GJ/年,其供热面积增加为262万m2,年增收节支2900万元.

Abstract

The recovery of exhaust steam waste heat for heating in thermal power plants can significantly reduce the cold-end losses of the unit.This paper proposes a method to retrofit power plant units by extracting exhaust steam and using a steam injector to eject it for heating purposes.The results indicate that under rated conditions,589 t/h of latent heat from exhaust steam can be recovered,reducing the annual average standard coal consumption for power generation of the No.2 unit by 61 g/(kW·h),increasing the heating capacity of the entire plant by 131 MW,and expanding the heating area by 2.62 million m2.After retrofit with exhaust steam,the heating capacity of the unit is increased by 131 MW,with a corresponding increase in heating output of 1.34 million GJ/year.This translates into an expanded heating area of 2.62 million m2 and an annual increase in revenue and cost savings of 29 million yuan.

关键词

冷端损失/乏汽/高背压/增汽机

Key words

cold-end loss/exhaust steam/high backpressure/steam injector

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出版年

2024
仪器仪表用户
天津仪表集团有限公司,中国仪器仪表学会节能技术应用分会

仪器仪表用户

影响因子:0.255
ISSN:1671-1041
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