油田化学2024,Vol.41Issue(3) :531-536.DOI:10.19346/j.cnki.1000-4092.2024.03.021

黄3长6区集输站结垢机理与防垢措施

Scaling Mechanism and Anti-scaling Measures of Huang 3 Chang 6 Gathering and Transportation Station

张道法 姬忠文 马琦力 徐琳 贾晨浩 贺波 刘婉
油田化学2024,Vol.41Issue(3) :531-536.DOI:10.19346/j.cnki.1000-4092.2024.03.021

黄3长6区集输站结垢机理与防垢措施

Scaling Mechanism and Anti-scaling Measures of Huang 3 Chang 6 Gathering and Transportation Station

张道法 1姬忠文 1马琦力 1徐琳 1贾晨浩 1贺波 2刘婉2
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作者信息

  • 1. 中国石油天然气股份有限公司长庆油田分公司第五采油厂,陕西西安 710200
  • 2. 中国石油集团工程材料研究院有限公司,陕西西安 710077
  • 折叠

摘要

为了解决黄3长6区采出水结垢导致管线、设备堵塞而严重影响集输站运行的问题,通过对集输站和单井的水样、垢样进行分析,明确了黄3长6区结垢原因,针对性地开发阻垢药剂,并报道了现场应用情况.黄3长6区集输站垢堵严重的主要原因是单井采出水不配伍,导致站场集输系统硫酸钡锶结垢堵塞.开发的高效钡锶阻垢剂(HDTMPA、P-M-P(5000)质量比为4∶1),在加量为60 mg/L的情况下,对硫酸钡的阻垢率达到90.9%.室内适用评价实验表明,该阻垢剂对集输站A、B汇管模拟水的阻垢率高达90%和93%.现场应用结果表明,添加该阻垢剂可大幅降低A、B站场的结垢程度,有效解决了黄3长6区结垢问题,从而保障黄3长6区集输站长周期平稳运行.

Abstract

To solve the problem of scaling in the produced water of Huang 3 Chang 6 area,which leads to pipelines and devices blockage and seriously affects the operation of the gathering and transmission stations,the scaling mechanisms in the Huang 3 Chang 6 area was clarified through the analysis of water and scale samples from the gathering station and single well,and targeted scale inhibitors was developed,in addition,the application of the scale inhibitor in the field was mentioned.it was determined that the main reason for severe scale blockage in the Huang 3 Chang 6 area gathering and transportation station was the incompatibility of single well produced water,which leaded to barium strontium sulfate scaling and blockage in gathering and transportation system.A highly efficient barium strontium scale inhibitor,mass ratio of HDTMPA to P-M-P(5000)being of 4∶1,was developed.The inhibition rate of barium sulfate scale was 90.9%when the concentration of the scale inhibitor was 60 mg/L.The indoor applicability evaluation test showed that the scale inhibition rates of the scale inhibitor on the simulated water of the A and B gathering station manifold was as high as 90%and 93%,respectively.the on-site application test of the scale inhibitor showed that the scale inhibitor significantly reduced the scaling degree in the gathering and transmission stations stations A and B,indicating that the application of the scale inhibitor could effectively solve the scaling problem and ensure the long-term stable operation of the Huang 3 Chang 6 area gathering and transmission stations.

关键词

硫酸钡锶/结垢/堵塞/钡锶阻垢剂/阻垢率

Key words

barium strontium sulfate/scaling/blocking/barium strontium scale inhibitor/scale inhibition rate

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出版年

2024
油田化学
四川大学高分子研究所 高分子材料工程国家重点实验室

油田化学

CSTPCD北大核心
影响因子:0.868
ISSN:1000-4092
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