首页|GCr15轴承钢穿孔裂纹产生原因分析及改进措施

GCr15轴承钢穿孔裂纹产生原因分析及改进措施

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针对GCr15轴承钢在开坯时出现穿孔裂纹的问题,通过金相显微镜、扫描电子显微镜、FEI金属质量分析仪等手段,对穿孔裂纹产生的原因进行了分析,并提出了改进措施.结果表明:GCr15轴承钢在开坯时出现的穿孔裂纹起源于钢坯芯部,芯部裂纹周围无夹杂夹渣,组织正常,无过热过烧现象,说明钢坯加热温度正常,而芯部裂纹明显脱碳说明其出加热炉之前已扩展至钢坯表面,结合钢坯入炉前的抛丸探伤检验,判断其芯部裂纹是在加热过程中产生的;依据缺陷钢坯的宏观断面形貌及显微组织,GCr15轴承钢穿孔裂纹是由于其在开坯加热时钢坯降温至1 000 ℃以下补充煤气供应,后迅速加热升温至1 280 ℃轧制造成的,钢坯加热升温过快,出现"穿孔裂纹"的频率会大大提高.据此优化了开坯加热工艺,对于GCr15轴承钢出现煤气供应不足的降温问题,需待加热炉重新恢复加热能力后,按照预热段30~50 ℃/h的加热速率升温至1 000 ℃以上,使钢坯完全奥氏体化后再快速升温加热.采用此改进工艺,彻底消除了GCr15轴承钢开坯轧制过程中出现穿孔裂纹的问题.
Cause analysis and improvement measures for perforation crack of GCr15 bearing steel
Aiming at the problem of perforation crack in GCr15 bearing steel during break-down rolling,the causes were analyzed by the means of metallographic microscope,scanning electron microscope and FEI metal quality analyzer,and the improvement measures were put forward.The results showed that the perforation crack of GCr15 bearing steel originated from the core of the billet,and there were no inclusions or slag inclusions around the core crack.The microstructure was normal and there was no o-verheating and over burning phenomenon,indicating that the billet heating temperature was normal,while the obvious decarburi-zation of the core crack indicated that it had expanded to the surface of the billet before leaving the heating furnace.Combined with the shot blasting test before the billet was put into the furnace,it was concluded that the core crack was generated during the heating process.Based on the macro-morphology of the section and microstructure of the defective billet,the perforation crack of GCr15 bearing steel is caused by supplementing gas supply when it cools down to below 1 000 ℃ and then heats up to 1 280 ℃ for rolling quickly.The billet is heated too fast,and the frequency of perforation crack greatly increase.And based on this,the heating process is optimized.For cooling problems such as insufficient gas supply of GCr15 bearing steel,it is necessary to wait for the heating furnace to regain its heating capacity.For the first heating,the temperature should be raised to over 1 000 ℃ according to the heating speed of 30-50 ℃/h in preheating stage,so that the billet can be fully austenitized.And then the billet can be heated rapidly.The adoption of this improved process can completely eliminate the problem of perforation crack during the hreak-down rolling process of GCr15 bearing steel.

GCr15 bearing steelbreak-down rollingheating technologyperforation crack

董庆、张育明、秦耀宗、范振霞、赵昊乾

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河北邢钢科技有限公司,河北 邢台 054799

邢台钢铁有限责任公司,河北 邢台 054027

河北省线材工程技术创新中心,河北 邢台 054027

GCr15轴承钢 开坯轧制 加热工艺 穿孔裂纹

河北省科技计划项目

205676134H

2024

轧钢
中国钢研科技集团有限公司

轧钢

CSTPCD北大核心
影响因子:0.881
ISSN:1003-9996
年,卷(期):2024.41(3)
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