钻井液与完井液2024,Vol.41Issue(3) :405-413.DOI:10.12358/j.issn.1001-5620.2024.03.017

滑溜水压裂液用超疏水型多功能减阻剂制备及应用

Preparation and Application of Superhydrophobic Multifunctional Drag Reducing Agents for Slickwater Fracturing Fluids

冯奇 蒋官澄 张朔 黄胜铭 王全得 王文卓
钻井液与完井液2024,Vol.41Issue(3) :405-413.DOI:10.12358/j.issn.1001-5620.2024.03.017

滑溜水压裂液用超疏水型多功能减阻剂制备及应用

Preparation and Application of Superhydrophobic Multifunctional Drag Reducing Agents for Slickwater Fracturing Fluids

冯奇 1蒋官澄 1张朔 2黄胜铭 1王全得 1王文卓3
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作者信息

  • 1. 油气资源与探测国家重点实验室·石油工程教育部重点实验室·中国石油大学(北京),北京 102249
  • 2. 渤海钻探井下技术服务分公司,天津 300457
  • 3. 中海石油(中国)有限公司湛江分公司南海西部石油研究院,广东湛江 524057
  • 折叠

摘要

目前常规滑溜水压裂液体系普遍具有减阻、携砂、抗盐和耐温等多种功能,但均没有考虑通过改变储层表面润湿性而实现储层保护功能.因此,以丙烯酸、丙烯酰胺、自制材料 2-丙烯酰胺基-2-苯基乙烷磺酸和疏水改性剂等为原料,合成了一种超疏水型多功能压裂液用减阻剂SHJZ-1.通过红外光谱仪对合成产物减阻剂结构进行表征,且通过高温高压岩心动态损害评价系统、接触角测量仪、哈克流变仪、闭合管路摩阻测试仪等方法对其性能进行综合评价.结果表明,该减阻剂 SHJZ-1溶解时间短,起黏快;当盐水的矿化度达到 40 000 mg/L时,0.5%SHJZ-1溶液的减阻率在 68%左右;0.15%SHJZ-1溶液在 140℃下高温老化,减阻率仍能达到 70%以上;1.3%SHJZ-1溶液处理后的岩心表现出超疏水效果,岩心接触角为 151.21°;该减阻剂溶液对岩心平均渗透率伤害率仅为 11.6%.超疏水型多功能压裂液体系在HX-1井顺利进行了现场应用,压裂过程中压裂液性能比较平稳,压后产量与临井相比提升10%以上,实现了提质增效的目的.

Abstract

At present,conventional smooth hydraulic fracturing fluid systems generally have various functions such as drag reduction,sand carrying,salt resistance,and temperature resistance,but none of them have considered achieving reservoir protection by changing the surface wettability of the reservoir.Therefore,in this paper,a superhydrophobic multifunctional fracturing fluid drag reducing agent,named SHJZ-1,was synthesized using acrylic acid,acrylamide,self-made material 2-acrylamido-2-phenylethanesulfonic acid,and hydrophobic modifier as raw materials.The structure of the synthesized drag reducing agent was characterized by infrared spectroscopy,and its performance was comprehensively evaluated through various methods such as high-temperature and high-pressure core dynamic damage evaluation system,contact angle measurement instrument,Hack rheometer,and closed pipeline friction tester.The results show that the drag reducing agent SHJZ-1 had a short dissolution time and rapid adhesion.When the salinity of saline water reaches 40000 mg/L,the drag reduction rate of 0.5% SHJZ-1 solution was about 68% .The 0.15% SHJZ-1 solution can still achieve a drag reduction rate of over 70% after high-temperature aging at 140℃.Furthermore,the core treated with 1.3% SHJZ-1 solution exhibited superhydrophobic effect,with a core contact angle of 151.21°.Additionally,the average permeability damage rate of the core caused by this drag reducing agent solution was only 11.6% .The super hydrophobic multifunctional smooth hydraulic fracturing fluid system has been successfully applied on site in the HX-1 well.In fracturing engineering,the performance of smooth hydraulic fracturing fluid is relatively stable,and the production after fracturing is increased by more than 10% compared to the adjacent well.The effect is significant,achieving the goal of improving quality and efficiency.

关键词

滑溜水压裂液/减阻剂/超疏水/现场应用

Key words

Slickwater fracturing fluid/Drag reducer/Superhydrophobic/Field application

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基金项目

国家自然科学基金重大项目(51490653)

出版年

2024
钻井液与完井液
中国石油集团渤海钻探工程有限公司 中国石油华北油田公司

钻井液与完井液

CSTPCD北大核心
影响因子:1.079
ISSN:1001-5620
参考文献量23
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