钻井液与完井液2024,Vol.41Issue(4) :551-556.DOI:10.12358/j.issn.1001-5620.2024.04.018

一种聚合物凝胶暂堵剂的研制及其应用

Development of Polymer Gel Temporary Plugging Agent and the Application

刘文堂 刘昱彤 李旭东 刘云飞
钻井液与完井液2024,Vol.41Issue(4) :551-556.DOI:10.12358/j.issn.1001-5620.2024.04.018

一种聚合物凝胶暂堵剂的研制及其应用

Development of Polymer Gel Temporary Plugging Agent and the Application

刘文堂 1刘昱彤 1李旭东 1刘云飞1
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作者信息

  • 1. 中石化中原石油工程有限公司钻井工程技术研究院,河南濮阳 457001
  • 折叠

摘要

老君 4井为普光边缘的一口高含硫气井,经酸压后,地层压力系数低,液面亏空达 1200 m,需进行高强度暂堵后才可进行投产作业,且该井安装两个间隔 1m且内径小(45 mm)循环阀,常规暂堵剂无法顺利通过循环阀内径.针对以上难题,以AMPS、AM为单体,复合一定粒径的无机材料,协同盐和除氧剂等材料,开发出了聚合物凝胶暂堵剂并在老君 4井进行了成功应用,室内和现场实验表明:聚合物凝胶暂堵体系 130℃下高黏度维持时间长达 15d以上,封堵承压达27 MPa,可阻滞高含硫气从井筒逸出,解堵率高,投产后产量约1.20×106 m3/d,应用效果良好.

Abstract

Laojun 4 Well is a high sulfur gas well located on the edge of Puguang,after acid fracturing,The formation pressure coefficient is low,before putting into production,the temporary plugging is necessary,but there has two Circulation valves stalled within 1m,the normal temporary plugging agents cannot smoothly pass through the inner diameter of the circulation valve.In view of the above problems,a polymer gel temporary plugging agent has been developed and successfully applied in Laojun 4 Well.Laboratory and field experiments show that the polymer gel temporary plugging agent has a plugging pressure of 27 MPa and a validity period of 15 days at 130℃,with the high plugging removal rate,it can block the gas escape from the wellbore.After being put into production,the output is about 1.2 million m3/d,the effect of site application is super.

关键词

聚合物凝胶/暂堵/滞气/封堵

Key words

Polymer gel/Temporary plugging/Gas stagnation/Plugging

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基金项目

中原石油工程公司科研项目()

出版年

2024
钻井液与完井液
中国石油集团渤海钻探工程有限公司 中国石油华北油田公司

钻井液与完井液

CSTPCD北大核心
影响因子:1.079
ISSN:1001-5620
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