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某发动机后处理装置气流再生噪声分析与改进

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为降低某发动机后处理装置气流再生噪声,采用计算流体动力学(computational fluid dynamics,CFD)建立后处理装置气流再生噪声有限元模型,进行噪声源强度分析,确定气流噪声最大声压级在出口管后排穿孔处.设计出口管穿孔结构改为插管结构和封堵后排穿孔2种优化方案,进行声压级及传递损失仿真对比;将采用封堵后排穿孔的后处理装置结构与原方案进行车辆加速行驶测试对比.仿真结果表明,2种优化方案的气流噪声声压级均降低,且不影响后处理装置降噪能力.测试试验结果表明,采用封堵后排穿孔的后处理装置结构,噪声明显降低,由流体流动引起的宽频噪声几乎消失,噪声总声压级由原来的90.4 dB下降到82.3 dB.
Analysis of airflow regeneration noise in an engine aftertreatment device and its improvement
In order to reduce the airflow regeneration noise of an engine aftertreatment device,a finite element model of the airflow regeneration noise of the post-treatment device is established using computational fluid dynamics(CFD).The intensity of the noise source is analyzed,and the maximum sound pressure level of the airflow noise is determined at the perforation in the back row of the outlet pipe.Two optimization schemes are designed:changing the perforation structure of the outlet pipe to an intubation structure and blocking the perforation in the back row,and the sound pressure level and transmission loss are compared by simulation.A comparison is made between the structure of the aftertreatment device that blocks the rear perforation and the original design by vehicle acceleration testing.The simulation results show that both optimization schemes reduce the sound pressure level of airflow noise,and do not affect the noise reduction ability of the post-processing device.The test results also show that using a aftertreatment device structure to seal the rear perforation significantly reduces noise,and the broadband noise caused by fluid flow almost disappears.The total sound pressure level of the noise decreases from 90.4 dB to 82.3 dB.

engineaftertreatment deviceair flow regeneration noisetransmission loss

崔志勇、陈志响、王宁波、马庆镇、翟旭茂

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潍柴动力股份有限公司,山东潍坊 261061

内燃机可靠性国家重点实验室,山东潍坊,261061

潍坊市应急救援服务中心,山东 潍坊 261061

发动机 后处理装置 气流再生噪声 传递损失

国家重点研发计划

2021YFD2000302

2024

内燃机与动力装置
山东省内燃机研究所 潍柴控股集团有限公司

内燃机与动力装置

影响因子:0.192
ISSN:1673-6397
年,卷(期):2024.41(2)
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