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催化裂解装置回炼重整碳五油的工业试验

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在中海石油宁波大榭石化有限公司22万t/a催化裂解(DCC)装置上进行了重整碳五油回炼的工业试验.结果表明:回炼过程中装置运行稳定,在提升管出口温度为620℃的条件下,重整碳五油转化率为42.90%,其中纯碳五转化率为25.65%;回炼重整碳五油后,DCC装置干气中的乙烯体积分数增加了0.55个百分点,丙烯收率增加了 0.12个百分点.
Industrial test of refining reformed C5 oil in deep catalytic cracking unit
The industrial test of refining reformed C5 oil recycle was carried out in a 220 kt/a deep catalytic cracking(DCC)unit of Ningbo Daxie Petrochemical Co Ltd,CNOOC.The results showed that the unit ran stably during the refining process,under the condition of the outlet temperature of the riser at 620 ℃,the conversion rate of reformed C5 oil was 42.90%,of which the conversion rate of pure C5 oil was 25.65%.After refining reformed C5 oil,the ethylene volume fraction in dry gas of DCC unit in-creased by 0.55 percentage point,and the propylene yield increased by 0.12 percentage point.

deep catalytic crackingreformed C5 oilrefiningethylenepropylene

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中海石油宁波大榭石化有限公司生产技术部,浙江宁波 315812

催化裂解 重整碳五油 回炼 乙烯 丙烯

2024

石化技术与应用
兰州石化公司石油化工研究院

石化技术与应用

CSTPCD
影响因子:0.491
ISSN:1009-0045
年,卷(期):2024.42(4)