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地震作用下预应力锚索在隧道洞口开挖加固效果评价

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本文以柿子园隧道为研究对象,对基于地震作用下的预应力锚索加固在隧道洞口开挖中的效果进行分析评价.结果表明,随着隧道开挖施工其稳定性安全系数有所降低,甚至一度降低至1.2611,这意味着隧道开挖过程造成内部应力分布发生转变,导致稳定系数随之减小.对洞口侧坡予以预应力锚索加固,安全系数较之前有所提升,施工安全性以及稳定性得到保障.加固措施实施后,结构变形速率等数值均处于可控范围,且洞内变形相对稳定.加固措施具有一定加固成效,能够提升和保证进洞施工的稳定性、安全性.
Evaluation on Effectiveness of Prestressed Anchor Cable Reinforcement Based on Seismic Action in Tunnel Mouth Excavation
Taking Persimmon Garden Tunnel as the research object,this paper analyzes and evaluates the effectiveness of prestressed anchor reinforcement based on seismic action in tunnel mouth excavation.The results show that with the excavation of the tunnel,the safety factor decreases,and the safety factor decreases to 1.2611,which means that the internal stress distribution state of the slope is changed by the excavation of the cave,resulting in the decrease of slope stability factor.The anchor cable is used to pre-reinforce the side slope,and the safety factor of the slope is increased compared with before,and the construction safety and stability are guaranteed.After the completion of the reinforcement measures,the structural deformation rate and other values are within the control range,and the deformation in the cave tends to be stable.The reinforcement measures have a certain reinforcement effect,which can improve and ensure the stability and safety of tunneling construction.

seismic actionanchor cable reinforcementprestresseffect evaluation

王建伟

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中铁十九局集团第六工程有限公司 江苏无锡 214028

地震作用 锚索加固 预应力 效果评价

中国铁建股份有限公司科技研发计划

2018-C18

2024

铁道建筑技术
中国铁道建筑总公司

铁道建筑技术

影响因子:0.539
ISSN:1009-4539
年,卷(期):2024.(6)
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